Charlie's first club event, a Fuel Economy Run and came home with a trophy.
Holly taking her Grandma for a Christmas Day drive.
Grandma was the inspiration for buying a 27 Chev, as she told Holly stories of family outings in her dad's 27 Chev when she was a child.
Following few pics are a brake and wheel restoration during COVID lockdown July - October 2020. After months of being on axle stands Charlie finally has all 4 wheels back on the ground. New Brake drums, linings, bearing and seals.
Removal of the engine went well with
every nut, bolt, washer and part being labelled and placed into storage. The
engine and gearbox were in the shed by 16 May 2021 and no time was wasted in
stripping them down.
As the gentleman who was going to rebore
the engine block and do the Babbitt bearings had gone on an adventure in his 28
chev (from Melbourne to Gulf of Carpentaria and back via Alice Springs), the
gearbox was first.
Some replacement gears were sourced from
a generous car club member and the gearbox was filled with a better second-hand
input shaft; better second-hand second and third gears; new counter shaft and
bushings; new reverse idler shaft and bushings and new bearings including an upgrade
to an aluminium main gear drive bearing retainer and modern seal.
While the engine was out a few other bits and pieces were restored
New clutch and brake pedal bushings were installed
while the pedals were off.As am sure happens often, when things
are pulled off a car, they get cleaned and painted and, when the engine and
gearbox get removed, there are a lot of parts that can be cleaned and painted.
This includes the gauges and, as the speedo wasn’t working properly, the speedo
was sent off for repairs. After several trips to the speedo repairer and a
couple of trips with the great club member, enough parts for a complete working
speedo were sourced and the gauges were looking great. A new speedo cable was
also made up at the same time. Now we will be able to see exactly how slow
Charlie is travelling. (more important is the fact that we will see how many
miles the new engine has done).
Still waiting on the engine meant plenty
of time to get everything else done – the Carter RAXJ-O carburettor was next up
for an overhaul. The carby looks great with its new jets, brass bowl and
polished brass connectors.
The vacuum tank also got some attention, and it was decided to move the vacuum tank on the firewall away from the
engine to allow easier access to the number 4 spark plug. This then
necessitated new fuel lines to the tank and from the tank to the carby and
inlet manifold.
With the engine back from the machinist
with new main and big end bearings; cylinders bored out 0.060”, new “high
compression” (LOL) pistons and rings and a cylinder head that was decked and modified
to accommodate Holden 308 valves which have a thicker valve stem. The valves
were shortened and modern valve spring retainers are used. The camshaft was
reground to standard profile so that it no longer resembled a horse saddle. Of
course, the engine needed to look good so it was cleaned, sanded and painted in
enamel.
A decision was made to use the original rocker
gear as it seems ok and can be replaced at a later stage if needed without
pulling the engine back out.
New head
bolts were installed as well a new timing gear, and camshaft thrust plate.
The oil pump was tested to make sure
that is pumps the oil into the splashers (not a lot of pressure is needed) and
the dippers on the end of the big end bearings were measured to ensure that the
oil system would work as intended. The sump was slightly bent where it had been
previously overtightened so that was straightened and painted. A real challenge
was encountered trying to get the sump gaskets and seals to stay in position
while the sump was bolted on (using new bolts).
A one piece replacement clutch was found
to replace the standard 1927 clutch plate which has the friction material
separate from the plate. The clutch plate appeared to be brand new so it was
cleaned and installed. A minor problem was encountered when a bolt broke when
tightening the pressure plate.
Thankfully, it came out easily and new high tension bolts were
installed. An upgrade was made to the clutch throwout bearing to replace the
standard carbon friction type to a ball bearing type. The flywheel didn’t need
any work except a clean and very light sand with some emery paper. The ring
gear showed no signs of wear so that was reused. A new clutch pilot bushing was
installed.
Before the engine and gearbox were
refitted to Charlie, a new bushing and seal were installed in the driveshaft.
With the engine rebuilt and attached to
the gearbox, it was time to reunite them with Charlie.
The installation was reasonably straightforward but it
required a bit of manoeuvring before it finally sat in place. The trickiest
part was trying to get the driveshaft on the correct angle.
Once the engine was sitting in, there
was only everything else to finish and the process of ensuring everything went
back where it was supposed to was made much easier thanks to the thorough
labelling process done when it was pulled apart. Nevertheless, there was still
many times where things had to be undone and looking at the photos taken during
the dismantling demonstrated that there is a lot to be learned and you don’t
know that you don’t know until you need to know.
New spark plugs, ignition points and
rotor and a distributor cap were installed – the distributor was checked for
excessive play in the shaft and appears to be ok. New pushrod felts were
installed above the cleaned and checked pushrods and new oils in the engine, gearbox
and uni joint were added. During the rebuild process, assembly lube was used
extensively.
Finally, after nearly 9 months, Charlie
fired back into life. It was only a
quick run to check for massive fuel or oil leaks and to check that the timing
was close. Surprisingly, fuel was fed to the vacuum tank quickly even though
the fuel tank had been emptied and the timing appeared to be spot on.
An electrical problem showed up and,
although the ignition wasn’t affected, the single fuse (behind the light
switch) kept blowing intermittently. After four or more hours of back breaking
circuit testing under the dash, the fault was traced to the horn that had been
dismantled and painted. It seems that it had been incorrectly assembled for
many years and there was a thick layer of dirt and grime that was acting as an
insulation. When that was all clean, it the incorrectly installed insulation
wasn’t working and the horn was shorting out. This is why the problem was
intermittent – the fuse only blew when the horn was pressed. With that problem
identified, the horn was further dismantled and the motor contacts and brushes
cleaned up and the horn has never sounded or looked better.
With the electrics sorted, it was time
to look again at the engine and to start some running in procedures. First up
was to adjust the clutch and make sure that the newly refurbished gearbox were
working. Unfortunately, the clutch appeared not to be engaging. As you can
imagine, this was most disappointing. Several hours were spent contemplating
this problem before it was decided that the gearbox had to come out.
With the gearbox out and the oil in the
uni joint slowing leaking out, a spare bell housing was used to investigate the
clutch. It appeared to look okay and the dimensions were (again) measured
against the original. It was suggested that a different pressure plate was required
before the problem was finally identified. The replacement clutch plate was
hitting the bolts holding the flywheel to the crank. As the pressure plate
presses the clutch plate against the flywheel, it was only possible to identify
this problem when the clutch pedal was installed. A second replacement clutch
plate was found in the cupboard and It cleaned up well. The gearbox was
reinstalled and filled back up with oil and lube (in the uni). The pedals were
reinstalled and the gearbox top (with the gear selector) was installed. With
the car still on stands another test of the clutch and gearbox was made.
Although the clutch pedal appeared to be moving normally, the gear stick could
not move to select gears.
This time, only the gear selector needed
to be removed and it was found that the gears had moved inside the gearbox
before it had been reinstalled. Finally, the gear selector was placed back with
the gears in the correct position and everything was bolted back.
As the gearbox and clutch now appeared to
be working properly, it was time to run the motor in. Five minutes running with
two very nervous people looking for leaks and listening for strange noises. A
couple of small water leaks have appeared – one form the outlet on the cylinder
head and one appears to be coming from the water pump adaptor that is used to
mount the modern Holden water pump.
A major fuel leak has appeared which occurs
only after the car has been stopped and the fuel tap it still on.
Once the pedals and floorboards were
replaced and the clutch pedal adjusted it was time for the first drive – about
a mile up the road and back. Success!
Although first and second gears sound louder than previous, the
engine appears to be running nicely. Some minor timing adjustments and the
valve clearances were done and Charlie is now back on the road.
Thats the story so far, more to follow I am sure, with a few videos
For more details on Charlie the 27 Chev Holly can be contacted at
schwindfamily4@gmail.com